Richards newly found race bike.......pt 3
First test run...
The
afternoon session was ideal for a first outing, long enough to get the feel for
what needed doing without having to miss sessions whilst attempting over
ambitious repairs/modifications. 3 x 20 minute outings spread over a 3 hour
period allowed us only time to attend to matters affecting running, other flaws
were noted for attention in the workshop on our return home.
Not only was this a test of the bike but also the new trailer & RMs
stock of tools & spares for the forthcoming trip to Schleiz
The
first attempt at starting was not encouraging, a push down the paddock gave not
a pop. Odd as it had been starting readily at home. What had changed? Only the
addition of the OE points cover. Removal of the offending item resulted in a
start on a set of rollers kindly offered by a near paddock neighbour. The
cover had been shorting out on the points terminal. The session went well with
the full 20 minutes being run. Towards the end the bike sounded flat & some
popping & banging was evident. On inspection the exhaust flange had loosened
& a lot of fuel dripping from the carb led us to think the fuel level was
too high. The second session revealed some oil seepage from the head area but
the bike ran very well in the first part of the run, in the later laps it
reverted to its flat sound again & a look at the plug revealed a
sooty covering with oil contamination. We dropped the fuel level a little
before the third outing but this was not to be the answer. The third
session allo
wed
a few more laps but the oil leaks were worsening & the mixture was
obviously
not right. Plenty to think about ,& some work needed before the first public
outing for the bike at Schleiz, but overall a very successful day with 60
minutes of running under the belt & no major problems.